We I got the call today and the damage was worse than I thought. The converter needs bushing, bearings and clutch plates. The good news is I can pick up the repaired converter tomorrow.
Converter Repair
February 19th, 2010 · Predator
I dropped off the torque converter at PhD Converters this afternoon. Unfortunately, I arrived to late in the day for them to cut the converter open while I watched. The plan is to Cut, Clean and Weld the converter, but I won’t know if there is any damage until Monday morning.
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More Tear Down Pics
February 16th, 2010 · Predator
These pictures are a little late, but I wanted to share them any how.
Not sure what she is looking for, but I hope she finds it.
Bearing damage from Crankshaft flex.
Right side pistons look okay, except #8.
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Another Boat Anchor
February 7th, 2010 · Predator
The original block was inspected by Brian at Thomson Automotive , anyone need a boat anchor? Mike dropped off a good bare block. The new block will be zero decked, bored .010 or .015 over, new billet 4-bolt splayed mains will be installed and the block will be line honed.
We’re looking at new pistons from Diamond and JE. Hopefully, we can find some the will allow us to lower the compression ratio and have a little more material around between the dome and the top ring groove.
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Notes from Mike
February 5th, 2010 · Predator
Brief History of engine, Original Specs.
Original Engine built by Combination in 2005.
2-bolt main LT1 block, 0.040″ Over, hence 384.6 ci, which I’ll round to 385.. Zero-decked.
Billet splayed main caps on #2-3-4 mains.
ARP head and main studs
Eagle Forged crank, and H-Beam Rods
Custom JE Forged pistons – build sheet does not list the dish volume, I will have to cc a good piston to see what it is.
Ported Iron Heads
ATI Procharger running 9-16# of boost, depending on how much the belt was slipping.
I received the motor after it lost oil pressure. The motor was run for ~1 mile before it got shut down (Note to self: put a frickin HUGE oil pressure warning light on the dash so you notice it even when driving in busy traffic with screaming kids in the back seat..). Needless to say, motor came out.
Here’s why it lost oil pressure. Note the offset to the pump gear teeth. Not sure what the debris was, but it was hard enough to not get chewed through the pump, and small enough to get through the pickup screen.
Pump shaft was bent too.
Pulling main caps to see how FUBAR’d the bottom end was… not as bad as we thought it would be.
Minor embedded material in the #1 cap, I have seen much much worse.
Hmmm….. not too bad.
Things got a little warm in there, note the bearing shrunk in. While it got hot, it DID not spin. Copper was showing on this one.
#5 looked the worst, but still looked decent, if the rod journals look good, this might not be too painful. New pump, polish the crank, new bearings and gaskets, … put it together……….. a strong example of why forged cranks are nice… kill bearings but the crank stays decent. Nice hard journals. A few hundred bucks and we are back in business
But what stuck the pump in the first place???? Time to pull the heads..
All 8 bores are scuffed, I’ll upload pics tonight maybe.
Hmmm, #8 piston looks a little funny..
Ruh Roh…
Heavy detonation on the crown.

Top ring land was flared up near both sides of the broken away portion.
More pics tonight… to be continued.
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Transmission Damage
January 25th, 2010 · Predator
I just picked up the transmission from Rik at Ortonville Transmission. Well the transmission damage was worse than I thought. Broken bolts in the overdrive housing, intermediate clutch pack was cooked, overdrive clutch damage. TCC solenoid screen was full of converter clutch material. The filter was clogged up with a combination of transmission clutch and converter clutch material.
If there was any doubt before, the torque converter definitely needs to be rebuilt.
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Piston Damage
January 25th, 2010 · Predator
Over the weekend Mike pulled the motor apart and sent me the following picture. Forunately, it doesn’t appear to have damaged the head. Mike is going to disasble the heads and inspect the seats just to be sure.
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‘Wha’ Happened’…
January 23rd, 2010 · Uncategorized
You may have noticed that the focus of the Predator-Racing website has changed. When Rik told me he had decided to take down the Predator-Racing website, I convinced him to allow me to take over the site and change to focus to Racing the Predator. In my mind Predator-Racing will always be Rik. I’m just keeping the lights on while Rik is busy taking on a new challenge.
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97.1 Video
January 22nd, 2010 · Predator
While cleaning up some old files I found this video of the Predator doing a burn out for the Deminski & Doyle show, back when they we on 97.1.
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4L80E Trans Rebuild
January 20th, 2010 · Predator
When I picked up the Predator the trans was out and the motor was damaged. The trans fluid smelled burnt, the color was off and there was some sediment floating in the fluid. No reason to take a chance, so I dropped it off for a rebuild. I’ve been using Rick’s Orion Transmission in Ortonville. The torque converter will go out shortly to be cut open and flushed.
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